Facebook slapped me in the face with this this morning:
…so I went on a mission.
I pulled the tank (for the millionth time?) and set up the 955i Triumph Tiger so I could try many different things to test if the idle was working. Previously I’d followed the manual, but no longer!
I did the usual checks for vacuum leaks and I continue to suspect the overly complicated and no longer supported idle control system. After trying everything I’d tried before, I decided to go OFF BOOK.
If I can’t fix this @*&%ing thing perhaps I can hack it! With the bike in test mode (plugged in and ready to run with all sensors attached), now is the moment to try some alternatives, so I pulled the entire idle control system and tried variations without it.
I plugged the servo back in because I figured leaving it unplugged might piss off the computer. I also removed the end of the servo so it wouldn’t interfere with the airbox and then blocked off the airbox with Gorilla Tape.
I’d also done my due diligence by balancing the throttle bodies and making sure everything else was plugged in as normal. I also reflashed the computer through Tuneboy with the South African map I found a few years ago.
So what happens when you remove the entire (problematic) idle control system in a Triumph 955i engine and simply connect the vacuum tubes out of the throttle body to each other?
Well, it seems to have fixed everything. The bike idles right where the computer sets it, the backfiring problem is gone and the motor fuels smoothly (though this is probably in large part due to that fantastic South African fuel map). Best of all, no more stalling.
That’s the work around. I got some silicon tubing from Amazon along with some T connectors (maybe $30 all in?). The last round of Triumph replacement parts cost me north of $200 and when I had to start buying used parts (because Triumph has stopped supporting their own bikes) and getting them shipped over to Canada it cost even more… but this hack is thirty bucks in parts and I also have a pile of unused silicon tubing and T connectors left over. I attached the silicon hoses to the T connector and then into each of the throttle bodies, so it’s a closed loop with no chance of leaks.
In the pic you can see the idle control servo (black object above the intakes on the left side). That’s what it looks like with the plunger removed. It still moves up and down but has nothing to do with moderating vacuum between the airbox and the throttle bodies which is what has caused me years of headaches.
I’m so jumpy about the motor falling through idle and stalling (it’s a perilous place to be when you’re on the road on a bike that keeps cutting out), but this hack hasn’t just solved the idle problem, it has also resolved all of the other issues. The bike idles steady right where I set it in Tuneboy, but more surprising is that the backfiring that had crept in is completely gone. The bike feels tight, full powered and like it did years ago. My only thought now is that it might hurt the gas mileage, but I’ll keep an eye on that as I get some miles under me this summer.
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